Canadian oddy, you are excellent. Thank you for digging in on this issue. I sincerely appreciate the effort.
Bugeye59 brings up a good point as well. I will go down the list of things mentioned since my last post.
Indeed, I have read may of the horror stories regarding air cooled
Engine failure. I have also read quite a few in which people have run their machines form many years without failure. Perhaps this is luck of the draw? Either way my goal when I began the rebuild was to get the machine running as it was from the factory and go from there. I was really trying to get familiar with the stock setup before introducing more variables. So on to the meat...
Now that you mention it, I had forgotten that the minimum octane ratings were based on leaded fuel. I am well aware of the benefits of the lead in relation to detonation. I just kind of pushed that fact aside because leaded fuel isn't an option. Also thinking that there have been improvements to the unleaded fuels of today to help mitigate detonation. As well as like you mentioned, many folks are running pump gas in their machines. That said, running a higher octane fuel is probably something I should consider for the long run.
The drive belt is brand new. In fact, just about everything on the machine is new. I literally have my heart and soul in to this thing. Every part was torn down, sand blasted, and painted. Every seal, bearing, and gasket in both the Engine and trans have been replaced, even packed the crankcase seals with fuel resistant grease as recommended. I swapped all of the hardware for stainless steel with the exception of the grade 5 & 8 fasteners. New u joints, new wheel bearings, the front arms were reworked by those cats out in Arizona. I ordered new Heim joints from the UK for the rear trailing arms and camber adjusters. New Works shocks at all four corners. The brake system has been completely rebuilt front and rear, along with stainless lines. I also replaced all of the crappy electrical connectors with GM weather packs. Seriously, name it and it has either been replaced, re-built, or re-worked. Mechanically the buggy is as good or better than the day Honda floated it over to the States back in '85. So I'm sure you can understand my dismay with the driveability.
Thanks for that link to the thread on jetting the PWK35. Definitely seems like I should be in the ballpark with the current jetting.
I will have to look into the throttle cable adjustment again. I suspect that this could at least be a contributing factor.
As far as pressure testing the bottom end, this is one thing I did not personally have my eyes on. But, the guy who bored the cylinder the second time did pressure test it after he put the Engine back together. Not sure of his procedure or what the actual number was, but he told me that it was all good. Things could have changed over the past year I suppose. However, an unmetered air leak should cause a lean condition and I really believe that my issue is too much fuel or not enough air in the problem throttle range.
I do not have access to another carb without buying another one. Small possibility that there could be an issue with the airstriker, but very slim. It is a brand new unit. Not sure what the last guy did to the stock carb, but no matter how small of a main jet I put in it, it ran pig rich. I even blocked off the fuel enrichment circuit completely to rule out the choke as an issue. Nothing helped. I think something was done internally to it. She would blow smoke like a freight train and go about 2 MPH. I only found out that it was junk by cutting the fuel supply and letting the carb drain the float bowl. The machine would finally pickup speed and power when the carb was almost out of fuel. That is when I switched to the new carb, and all of those issues went away. So I parted out the stocker and scrapped the body. I have no backup.
As fas as EGT and CHT measurement, CHT is measured via a plug sensor, and EGT is measured by a probe in the exhaust just past the first elbow after the exhaust manifold. Maybe not super accurate, but a decent picture of what is going on.
I have not performed a fuel volume test. Didn't see it as necessary being that the pump is new, and the return line is always full. I will do this test to rule it out. The tank is clean, had it clean and coated by a radiator shop. The fuel filter is always clean as well.
The airbox I put together could be a problem, at least where the issue lies. I will post some pics of this later when I get a few minutes. It could be starved for air under a heavy load. However, I can't run it with the lid open because it runs so lean at low revs that I can't even get past 1/4 throttle. I do need to dig into this. Maybe I will attach a rope to the lid so I can open it above half throttle and see what happens.
I really believe my problem is rich vs lean. I have not done a plug chop per se, but I have put a new plug in every time I have changed jetting. I check the plug after every run and it is always black with carbon on the electrode.
Sorry for the extensively wordy reply, but I'm trying to give everyone as much info as possible.