The air screw was out about 3.5 turns. I backed it out to 1.5 and then .5. The throttle response seemed quicker, but the machine still took about 5 secs or so to slowly idle back down from a slight rev.
The pulse tube appears to be original, it is pretty ratty looking and I already tried to change it but could not manage to remove it from the case easily. I only checked it by disconnecting it and checking for pressure with my thumb, while turning over the Engine. it appears to be working, but I would not be surprised if there was a leak in the line. I will have to work more on swapping it out, do you think using new fuel line hose will be ok for that? I bought lots of it, but The current line appears to be braided.
The intake manifold is probably original also, but it does not look as bad. It was pretty greasy and I cleaned it with some
Engine degreaser, I can see about half of its surface now, but it does not appear to have any cracking at all. I will give it some more cleaning and see what I can discover. I guess now would be a good time to check the reeds now anyway.
One more note about my setup, I do not think it will matter but the gas tank is so rusty that I have made an improvised tank using a small 2 gallon gas can and sticking the fuel line in its spout. If the machine is worth rebuilding I will likely just get an after market tank. The testing setup I have created is not using the T connector or overflow line and is using a replacement fuel pump with a new fuel filter. I can see gas moving through the filter so fuel supply does not seem to be an issue.