Thanks for the reply.
I
think my cylinder had been decked on a previous bore, before the sleeve. Then when the sleeve was installed, the guy wasn't paying attention, and just seated the sleeve flush with the top of the cylinder (without decking the sleeve to match the previously decked cylinder, this set the sleeve too low), matched up the porting, and bolted it together, which caused the sleeve to move upwards.
If I could get a total length of the stock sleeve, I could verify this, but I don't know what that number is.
The
Engine builder didn't drill the lube holes in the piston or relieve the exhaust bridge either, which leads me to believe he didn't really know what he was doing. Supposedly some guy down in Oregon, around Eugene, that "specializes" in FL350's and has a bunch of parts, but not an actual business. Don't know who he is, this is what the PO told me.
It's not too surprising that the sleeve was able to be moved, each of those M10 cylinder base bolts is exerting over 10,000 lbs of clamping force when torqued up, basically acting as a 40,000 lb press when the cylinder was bolted to the cases. Yeah, that'll move a sleeve.
I was able to remedy the situation last night by positioning the sleeve flush with the head gasket surface, removing .035" from the bottom of the cylinder sleeve, and matching up the porting a bit better. Logically, this lowered all the ports by .035", but with the porting that was done, the ports were raised by more than that anyway.
We'll see how it runs. If my measurements are right, I should end up with .080" squish band using the stock head and base gaskets, which is some improvement from stock anyway. I'm hoping to not need race gas in this; but compression was 165 psi cold, before I took the
motor ((
Internal Combustion Engine ? )) apart. I'm hoping there was something just funny going on to make the reading higher.