nickRNR wrote:
Well, the trip was a success. Had a great time, got some good riding in, got PPP's pilots dialed in for the most part, and most important, niether one of his pilots "Popped" LOL...cant say the same for the EEE though. Some of the high points of the trip...
My pilot: plug chops looked good, no re-jet
EEE: plug chops looked a bit lean so went to bigger mains, everything else looked good.
PPP's stock pilot: needed no re-jetting after reading a few plug chops, ran great all weekend no issues.
PPP's modified pilot: needed major re-jetting, pulled carb, tore down and cleaned after seeing some bad lookin stuff in the slide area, went from a 185 main to a 200 main, a 40 pilot jet to a 45 pilot jet, #4 groove on the needle (second from the bottom), and his air/fuel screw was only about 3/4 of a turn out, set it to 1&1/2 out. Jetting turned out to be DEAD ON! Damn, guess I'd rather be lucky than good HA HA! His pilot ran good, but after a while it was acting like the floats were stuck, turns out his fuel line was falling apart and chunks of crap were in the carb making the float valve stick, replaced fuel line, cleaned carb, but must have been more crap we didnt see, also had a rear tire leaking, got some good rides out of it, by that time the trip was pretty much over anyway.
Got some rain friday night along with 900mph winds, blew the trailer all over the damn place. Dunes got tore up a bit, but we still rode. Hell, we rode in the rain! Rained a bit saturday night too.
Threw the dirt tires on the UTV's and hit Sperry Wash, it was full of water and was really cool, tons of fun tromping though the streams.
Went to little dumont, met up with some of PPP's friends. Hung out for a bit, then headed back to camp.
Trip ended sunday night for PPP and his crew, they packed up and went home, they had to prep for their trip to Spain...bastards!!!! lol
Monday we visited the mine over at little dumont. Rode the little dunes a bit as well. Had fun. Returned to camp and finished loading stuff up, went to start the EEE, and she no go! Ran fine all weekend, and she didnt want to fire to come home. Guess she didnt want to leave!
Got home, unloaded stuff, got to work on the EEE today and come to find out the head gasket on the magneto side is blown, water leaked out through the exhaust, leak down test showed ok otherwise, compression is at 135 each side, so new head gaskets should cure the beast.
Anyway, trip was fun, had a blast, wish we could get more guys to ride.
PPP told me he got some really good videos, so will be waiting for those to show up on youtube. I got some "ok" ones, will post them later.
"bad lookin stuff in the slide area"
What did it look like?
What kind of carb?