I wanna ride. Well had some time in between jobs and a nice weekend . Got all the parts together THANKS TO ALL on this forum.
With much thought and a little patience a lot of blaster extra parts and some freebies from newly found friends I brought a fl350
back from the dead! For an initial investment of $800 bucks plus some extra bucks for parts cylinder hone and a piston dam those are expensive. Got buggy 1 going . A great big shout out goes to mark and rich for helping a newbie with a few of the technicals.
Took forever to get her cranked up and started but once she fired its starts every time.
Heat cycled . No wait, I am missing the middle of the story . Stix prodded me along on this I have never been to little sahara much less
went trail riding in a odyssey . So with the parts horded and knowing the trip is coming up this weekend gave me the incentive to get
going on the buggy. With piston prep done cylinder bored exhaust relief done cylinder head holes chased with a tap I was ready to tackle my project.
At about 5:00 fri got started. With the D.H. (that's me) crankcase breather treatment a little tubing bender would have made this go a little easier. Pics of that coming soon. Next assemble top end. O snap what did I do with that precious metal base gasket I got from
speedchaser my shop looks like a bomb went off, that was like finding a needle in a hay stack. It was in the tool box. Now to get the rings into the bore crap cant find my ring compressor, just so u know in a pinch 2 zip ties works well but is a bitch to get snugged up firmly enough with 2 cycle oil all over you're hands kinda reminds me of 2 monkeys and a football. lmao It wasent so funny at the time. Jug on, time for the head now about 8:00 one of the 3 which 1 the top bottom middle, I chose the later for the head gasket.
All together done a leak test . Test good. Next compression test 143 ish
motor ((
Internal Combustion Engine ? )) out of buggy electrified starter with spare battery. ok good called mark to let him know where I was at He told me no no no use the small one confirmed by rich . Changed middle gasket out for the thinner gasket for the head. retest leak test good comp great 150 ish plus.
Somewhere in there new pull start rope. getting late goal is to have Engine in buggy brakes blead. next was to blead the brakes what a
pain in my butt fast forward to 3:00 saturday morning brakes blead good enough excellent rear ok front . Time to put Engine in that sucks by yourself 4:30 am time for exhaust carburetor . Had to put carb back together after soaking and cleaning and blowing it out . sunday 5:30 put battery in and charge. 6:00 shower. 3 hrs sleep go coach my little girls soccer game we won good 24 hrs .