Well Want to friends deer lease and the rain head messed it up worse than we thought.Tried to do some plug chops but don’t know if the straightaway I had was long enough to do a proper Job and it probably didn’t matter in the end anyway.
Started out with a 170 main jet, did a plug chop,and went down to 168 and did another plug chop.Pilot is not really bogging But it doesn’t have the power it should and it is missing at full throttle.
After 2nd plug chop I want to check the choke to make sure it was operating correctly and the whole Choke assembly pulled out of the carb when I went to pull it up.(Remember this is not the carb that I was running before but Keihin Chinese knock off.)so I screwed that back into the car. Was messing around with it some more and checked the air mixture screw and it was screwed all the way in,So I do not know how that would have affected the plug chops?
So it’s still not running worth a crap, see no difference in those two jets, so I start messing with the air mixture and that doesn’t seem to make any difference either.
So then I go down to a 160 Main jet and that just makes it run worse So I don’t even bother doing a plug chop.
It was time to go,So when I had 170 jet in it would it have made a difference if choke assembly was screwed all the way in And air mixture screw wasn’t screwed all the way in I don’t know.
I am still being very paranoid about the way the
Engine sounds.
It sounds fine when I am in neutral and a rev it up When driving it and giving it for throttle it doesn’t sound right, but what I’m hearing just could be because it’s not running right and it’s missing?
Checked compression and it’s great(186)so if something wasn’t right with Engine I would think it would show up in the compression reading Which if anything has went up since initial testing after rebuild.
I am going to ditch this carb and try another chinese knockoff(PWK 40) I bought and try it,if it’s still running like crap then I will go back to original carb