djscoutmaster wrote:
Update
- made a leakdown test kit, used it and it failed misserably. Held pressure for about 10-15 seconds max. I sprayed soaping water on every part i could find and no bubbles. The 2 places i could not reach where the crank seals. The cluch and pull start covers were both on. Ill find the leak before the teardown of the rebuild. (Video attached)
- the tank is clean but the res line is clogged, tried everything to unclogg it. No luck. Im buying an air compressor tommarow to try and blow it out and if that doesnt fix it ill be getting a new gas tank.
- cleaned air filter and air box, painted my air filter top.
- in an effort to remove the seat i tried removing the bottom seat bolts. Water started porring out of the bolts and 2 of the 4 bolts snapped(rusted) and 1 is stripped. Good news, now i know why my seat would never dry out...
Questions
1. What options do i have for stripped rusted broken seat bolts? Do most buy an!aftermarket seat?
1) Seat bolts
The oddys have a safety bolt. It's just a regular bolt with the threads milled off a bit near the end. This leaves about two threads at the very end. I don't use these because when you try to take them out the two threads at the end almost always brake off in the hole. No problem though. Just punch the broken bit out with a hammer and punch. Use some skill here, don't FN smash it with the hammer. The bit will come out easy. You may then have to re-tap the hole. You should be able to use the original bolt now. Any bolts you get out with the little safety thread at the end I would just grind off. If at any point the hole threads are shot then what I have done is weld a new nut on.
2) You said: the tank is clean but the res line is clogged, tried everything to unclogg it. No luck. Im buying an air compressor tommarow to try and blow it out and if that doesnt fix it ill be getting a new gas tank.
NO -- you can drill and tap the drain plug and pull fuel from there. Both my machines are like that now. Pic below.
3) Leak down test
Yup it failed according to that video. You can loosen the dip stick and soap around it to see if any bubbles. If yes then the double lip seal is shot. You will also have to remove the pull starter assembly so that you can soap the seal in there and check for bubbles.
Edit: I hope you had the piston in the down position or at least low enough that the ports were open. The reason is that if the piston is up at TDC (Top Dead Center) then the pressure slowly migrates to the combustion chamber through the rings. Piston must be down for an accurate test. In my opinion though, that pressure drop I seen in the video was unbelievably quick. I don't think it would drop that fast even if the piston was up.